Last revised: April 24, 2019
ATC - 25 Best Years -
(1958-83)
Album #
7-A.
(1972)
The money bag and gun were discovered by searchers near Peru, Indiana.
While in Marion Federal Prison, the hijacker and fellow inmate (also a
hijacker - see January 28, 1972) on May 24, 1978 attempted a prison
escape after a girlfriend hijacked a helicopter. The escape attempt ended
when the helicopter pilot grabbed the woman's gun and killed her. The
hijacker was paroled from prison in 2010. |
(Mid-Air
Collision)
-Wisconsin
The NTSB report stated that both crews could have been scanning
instruments in preparation for descent at the time of the collision. It
also noted that the decision by both flight crews to fly under VFR
rather than IFR and the fact that neither captain requested
in-flight advisories deprived both aircraft of air traffic control report.
(13
Fatalities) |
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![]() August 1, 1972 - Northeast Airlines merged into Delta Airlines. Northeast began as Boston-Maine Airways in 1931, and changed the name to Northeast Airlines in 1940.
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The pilot tried to lift off too early in an attempted takeoff from Sacramento Executive Airport. He was pulled from the wreckage and survived. The NTSB determined that the probable cause of this accident was the
over-rotation of the jet, which was the result of inadequate pilot
proficiency in the F-86 Sabrejet and misleading visual cues. |
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They had the plane flown to several locations in the USA and to Toronto, Canada before finally flying to Cuba. However, Cuban President Fidel Castro did not accept them into that country, and the hijackers next had the jet flown to Orlando, FL. The hijackers threatened to crash the plane into the Oak Ridge Nuclear Installation at McCoy AFB, Orlando, FL if their demands were not met. While stopped for refueling at McCoy AFB, the FBI shot out two of the jet's four main tires, prompting the hijackers to shoot and injure the co-pilot and forcing the Captain to take off. The hijacking came to an end when the plane landed on a partially
foam-covered runway in Havana. The hijackers were removed from the jet at
gunpoint by Cuban authorities and captured after attempting to escape.
Cuba returned the jet, crew, passengers and ransom money to the United
States. The hijacking lasted a total of 30 hours and covered 4,000 miles. |
Failure of the captain to properly fly the approach, leading to a loss of airspeed, stall, and loss of control caused the accident. (43 Fatalities) The crash was the first fatal incident involving a B-737, which entered airline service in 1968. There was a lot of controversy about this crash as the wife of convicted Watergate conspirator, E. Howard Hunt was killed. Michelle Clark, CBS news correspondent was traveling with Mrs. Hunt, and rumor had it that the Hunts were about to announce information about the Nixon white house and its involvement in the Watergate burglary. A large sum of money (between $10,000 and $100,000) was found amid the wreckage in the possession of Mrs. Hunt. Several pages of documentation are available for further reading at: http://spot.acorn.net/jfkplace/09/fp.back_issues/02nd_Issue/dhunt.html
Also on Wikipedia:
http://en.wikipedia.org/wiki/United_Airlines_Flight_553 |
(Airport
Collision)
-Chicago, IL
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![]() December 20, 1972 - Chicago O'Hare Airport collision between Delta Air Lines Convair-880 and North Central Airlines DC-9. -- (45 fatalities on NC, 88 on Delta)
ATC cleared the Delta Convair-880 to cross the runway while the North Central DC-9 was on its departure roll. North Central DC-9 rolling down the runway (1/4 mi. visibility) into the fog, the captain spotted the Delta flight and gave the order "Pull 'er up!" and he and the 1st officer pulled back on their control columns in an attempt to lift their DC-9 over the Delta CV-880. Although the DC-9 lifted into the air, it was too late to avoid contact with the CV-880 and they collided. The collision sheared off the tail of the four-engine Delta jet and caused the North Central craft to crash a short distance down the 10,000-foot runway. An explosion and fire erupted. Firemen said the bodies of the dead were charred beyond recognition. The DC-9 captain attempted to land, the main landing gear collapsed rearward, and the aircraft skidded on its belly onto a grassy area where it stopped and immediately burst into flames. (10 Fatalities) Visibility at the time of the crash was 1/4 mile. Earlier in the day, air traffic was restricted to outbound flights due to the fog. The NTSB found that the probable
cause of the accident was the failure of ATC to ensure adequate aircraft
separation during a period of limited visibility. It also noted that
non-standard terminology was used to expedite traffic flow and included
the omission of words, altered phraseology and use of colloquialisms. Lack
of clarity of wording on the part of the ground controller with Delta,
and the Delta crew's failure to request confirmation were the
major causes of the accident. The controller was confused as to the
location of the CV-880, and neither the controller nor the Delta
crew realized that they were referring to different run-up pads as the
holding area for the Delta CV-880.
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The pilots broke off their approach to Miami International Airport after the nose-gear light failed to illuminate, indicating that the gear was properly lowered.
While in a holding pattern at 2,000 feet over the Everglades, the captain bumped his control column, leading to the disconnection of the autopilot. All three crew members were focusing on the landing gear problem and the extinguished light, and failed to notice as the aircraft descended into the ground. 69 passengers and 8 of the 10 flight attendants survived this crash. Of the cockpit crew only the Flight Engineer survived. The swamp absorbed much of the energy of the crash, lessening the impact of the jet, and saved many lives as mud blocked many wounds sustained by survivors, preventing them from bleeding to death. The NTSB discovered that the autopilot had been inadvertently switched from altitude hold to CWS (Control Wheel Steering) pitch. In this mode, once the pilot releases pressure on the yoke the autopilot will maintain the pitch altitude selected by the pilot until he moves the yoke again. The captain probably accidentally leaned against the yoke while turning to speak to the Flight Engineer, and the slight forward pressure on the stick would have caused the jet to enter a slow descent. The altitude alert sounded to warn the pilots of an inadvertent deviation from the selected altitude, but went unnoticed by the fatigued and frustrated crew due to the crew being distracted by the nose gear light. Visually, since it was nighttime and the jet was flying over darkened terrain of the Everglades, there were no ground lights or other visual indications that the TriStar was slowly descending into the swamp. Pilot error was reported as the cause of the crash:
"the flight crew failed to monitor flight instruments during the final
four minutes of flight and failed to detect an unexpected descent soon
enough to prevent impact with the ground. Preoccupation with a malfunction
of the nose landing gear position indicating system distracted the crew's
attention from the instruments and allowed the descent to go unnoticed." |
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(1973)
February,
1973 - An
understanding was reached between the USA and Cuba that hijackers would
face punishments (up to 20 years) in whichever of the two countries they
were captured. |
![]() ![]() March 14, 1973 - President Nixon names retired Air Force Colonel/Pilot Alexander Porter Butterfield to become the 5th FAA Administrator. Butterfield
served in the U.S. Air Force, and was a member of the Sky Blazers jet
fighter acrobatic team.
He advanced to the rank of Colonel and attended the National War College. He earned a B.S. degree from the University of Maryland and a Master of Science degree from George Washington University. Butterfield served as the Deputy Assistant to President Richard Nixon
and revealed the existence of a White House taping system during the
Watergate scandal. (But, that's another story, and not relevant here.) |
Mid-Air Collision - Sunnyvale, CA
![]() April 12, 1973 - Sunnyvale, California - a Mid-Air collision between a NASA Convair CV-990 Coronado and a U.S. Navy Lockheed P-3 Orion occurred on approach to Naval Air Station Moffett Field, California. They collided just south of the airfield (intending to land on the same runway) on Sunnyvale Municipal Golf Course, killing 11 people on the CV-990 and five of the six on the P-3C. One Navy crewman survived. (16 Fatalities)
Neither plane was experiencing any problems, and the probable cause of this accident was attributed to pilot error. They could have been approaching separate runways. Another theory is that the air traffic controller cleared both aircraft to the same runway. Eight scientists and technicians were on the NASA jet flying laboratory. Both planes somersaulted before hitting the ground in a ball of fire. The Convair 990 flying laboratory was valued at $5
million. The Navy P3 Orion was a $9 million submarine chaser. |
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A TWA flight, landing just before the FH-227 reported getting caught in a strong updraft, and was forced to execute a missed approach, rather than land. The captain and first officer both survived the accident and the captain reported hail hitting the airplane, pulling up on the control stick, and seeing fire after impact. The cockpit area was clear of the main wreckage, as the FH-227 broke into several pieces. The aircraft was in a high nose-up attitude at impact. Although the crew knew thunderstorms were in the vicinity, the controller's lack of urgency seemed to lead the crew to believe they could land ahead of the storms. Investigators believed that high winds and a strong downdraft pushed the plane below the glide slope. The crew's evasive actions were not enough to prevent the plane from striking the ground. Investigator's questions why the air traffic controller had not indicated the severity of the storm to the flight and also why the crew had not requested a different flight path to avoid the storm.
(38
Fatalities) of the 44 persons aboard) |
The air traffic controller was busy handling a potential collision conflict between two other aircraft and neglected to clear the Delta DC-9 for the approach. The crew had to ask the controller for an approach clearance, which was given immediately, but more than a minute after the intercept vector had been issued. They were high and fast and almost over the outer marker and unable to stabilize the descent rate and airspeed, and descended below the glide slope and drifted away from the localizer course hitting a sea wall. The weather was partially obscured by fog, with a 400' ceiling, 1/2
mile visibility and light winds. The NTSB concluded that the flight
crew inadvertently switched to a 'go around' mode during the final
approach, instead of the appropriate approach mode. This caused confusion
and additional pressure, and contributed to the unstabilized approach and
deviation below the glide slope and decision height until it struck the
seawall and crashed. Also no altitude callouts were made by the crew
during the final approach. (89 Fatalities) |
The jet was cleared for an approach, and the pilot reported leaving 31,000'. (The last recorded transmission). The NTSB determined that the probable cause of the accident was the captain's deviation from approved instrument approach procedures resulting in the jet's descent into an area of unreliable navigation signals and obstructing terrain. The Cockpit Voice Recorder indicated that the crew discussed the requirements and specified minima for the ILS back course DME approach to runway 32, and that the captain did not plan to make a procedure turn. After calling out a DME reading of 29 miles, the copilot questioned the captain: "We should be a little higher than that our here, shouldn't we?" About 3 minutes later the jet struck Mt. Dutton. The 3-man crew and 3 'non-revenue' company employees lost their lives
in this crash.
(6 Fatalities) |
![]() Approach charts were also improved for other airports where situations exist similar to those in Cold Bay, including advice that NAVAID signals beyond 40 miles of the VORTAC are unusable below certain altitudes. NAVAID restrictions also now have notes that 'high terrain either side of final approach course within 4 miles of the airport.' |
Jim Croce was an American singer-songwriter who released albums
with ABC Records.
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The cockpit voice recorder revealed that the first officer was flying the plane while the captain advised him of headings and altitudes to navigate around the storm. Expressing concern that their position was unknown and what the terrain clearance was, the first officer, followed the captain's orders and descended to 2,000 feet. He then consulted an en route instrument chart and alerted the captain that they were too low: "Minimum en route altitude here is forty-four hun...". At that the recorder cut off as the plane struck Black Fork mountain. Because the Convair-600 had deviated around the weather, over 100 miles North, the crash site was not found until 3 days later. A search helicopter crashed while searching for the lost plane and 3 people died.
The NTSB concluded that the crew did not discuss the details of their intended route with Flight Service or activate the IFR flight plan from their airline dispatch to Flight Service. Under IFR they would have been tracked by radar or required to make position reports to en route controllers. The cause of this accident was the captain's decision to continue into instrument weather at night, his choice to not use nearby navigational aids to determine their position, and his decision to descend despite the first officer's concerns about position and terrain. Eight passengers and three crewmembers were killed.
(11 Fatalities) |
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The crew initiated an emergency descent and landed safely at Albuquerque International Airport 19 minutes after the engine failed. Evacuation slides were used to evacuate 115 passengers and 12 crewmembers. However, one passenger died and 24 persons were treated for smoke inhalation, ear problems, and minor abrasions. (1 Fatality) One passenger was partially sucked through a failed cabin window that had been struck by engine fragments. Efforts to pull the passenger back into the jet were unsuccessful and he was forced entirely through the cabin window. The body was not recovered until two years later when someone came upon his skeletal remains.
The NTSB said the probable cause was the disintegration of the No. 3
engine fan assembly as a result of an interaction between the fan blade
tips and the fan case, caused by the acceleration of the engine to an
abnormally high fan speed and destructive vibration. One theory is the
crew was experimenting with the auto-throttle system. |
1st 25 Years: | Pre-FAA | 1959 | 1962 | 1965 | 1967 | 1968 | 1970 | 1972 | 1974 | 1977 | 1979 | 1981 | 1982 |
Last revised: April 24, 2019
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